Welcome to the Home of All Aviation Professionals Worldwide

As an existing or future Aviation Professional, we welcome your connection with us on Facebook, Plaxo, LinkedIn or Xing. Join us using the links below:

LinkedIn: 18,034 members http://linkedin.aviationprofessionals.org
Xing: 404 members http://xing.aviationprofessionals.org
19,133 Professionals in Total as of October 20, 2010

If you are an existing professional, or someone who has the "Dream", please join us and take the opportunities offered to share with others who are just like you.

Friday, September 3, 2010

An Interesting Lesson for all Pilots - Business jet mishandled at Kerry

A Gulfstream IV was put at high risk when its flightpath was badly
managed by the crew as they were turning back to Kerry airport with a
minor fault, according to an Irish Air Accident Investigation Unit
report.

The "serious incident" on 13 July 2009 began just after the GIV
(VT-MST) took off from Runway 08 at Kerry, bound for London Luton, UK
when the captain's windshield cracked and the crew requested a return
to Kerry. The AAIU report criticises the pilots for poor crew resource
management leading to a serious loss of situational awareness.

After being cleared to return to Kerry, the crew initiated what they
thought was a descent for landing on Runway 26, but the aircraft was
paralleling the instrument landing system approach path to that runway
some 10km (5.4nm) to the south.

The crew had ignored the Kerry controller's advice for the return and
did not provide its specific intentions nor a requested position
report. Since Kerry does not have radar, the controller was unable to
provide vectors. Intervention in the aircraft's 1,300ft/min descent
with gear and flaps down came when a controller at Shannon radar
called Kerry on the telephone and said the aircraft should be told to
climb immediately.

As Kerry delivered that instruction, the aircraft's enhanced ground
proximity system alerted the pilots. The minimum height above the
ground that the GIV reached was 702ft (215m), still in cloud, says the
AAIU.

Kerry handed the aircraft over to Shannon radar, and Shannon vectored
the crew to intercept the ILS for Runway 26. It finally landed safely
at Kerry, but not without having to carry out a 360° turn before the
ILS approach because of confusion caused when the co-pilot programmed
the approach to Runway 26 at Luton, instead of Kerry, into the flight
management system.

The AAIU found that the No 1 engine had suffered severe damage to its
fan and blades in both compressors from ingestion of an unidentified
metal foreign object, but the crew had not reported this. The engine
subsequently had to be changed.

After landing and disembarking the passenger, the crew had started up
the engines again to test the No 1 because it was vibrating. The AAIU
said this test served no purpose and caused more harm to the engine.

Flightglobal's ACAS database lists the aircraft as owned by Sunrise
Air. It has been leased to Asia Aviation since May 2007.

Posted via email from Aviation Professionals dot Org

No comments:

Post a Comment